New Search
My WebLink
|
Help
|
About
|
Sign Out
New Search
Eugene/Springfield Water Pollution Control Facility 1984-1991
COE
>
PW
>
Admin
>
Execs
>
Executive non-confidential
>
Historical
>
Eugene/Springfield Water Pollution Control Facility 1984-1991
Metadata
Thumbnails
Annotations
Entry Properties
Last modified
6/5/2009 11:34:05 AM
Creation date
6/1/2009 12:27:55 PM
Metadata
Fields
Template:
PW_Exec
PW_Division_Exec
Administration
PWA_Project_Area
Miscellaneous
PW_Subject
Water Pollution Control Facility
Document_Date
7/31/1993
External_View
No
There are no annotations on this page.
Document management portal powered by Laserfiche WebLink 9 © 1998-2015
Laserfiche.
All rights reserved.
/
85
PDF
Print
Pages to print
Enter page numbers and/or page ranges separated by commas. For example, 1,3,5-12.
After downloading, print the document using a PDF reader (e.g. Adobe Reader).
Show annotations
View images
View plain text
Section F: EQitIPMBNT MAINTSNANCB <br />pretreatment comminutor, staff redesigned the <br />internal cam follower and machined and replaced <br />it with a solid aluminum/bronze rectangular slide <br />block. No further breakdowns have occurred, sav- <br />ing aconsiderable amount in repair costs and <br />equipment downtime. <br />GRIT COLLECTOR MECHANISMS <br />In the first few months of operation, the grit <br />collector mechanism broke several times and re- <br />quired special modifications. The original system <br />was designed without the guides that keep the grit <br />collector flights in place, which allowed the drive <br />chains to slip off the sprockets. By designing and <br />installing guides, maintenance staff was able to <br />correct the problem. <br />The original wear shoes for the grit collector drive <br />mechanisms were made of steel, which wore out <br />within a short time. They were replacedwith shoes <br />of polyethylene - a material that has a much <br />longer life. The new shoes will save a considerable <br />amount of money in replacement and repairs costs <br />and in equipment downtime. <br />COMBUSTIBLE GAS MONITORS <br />Staff installed a continuous combustible gas moni- <br />tor and an alarm system at pretreatment to wam <br />employees if an industrial spill occurs. <br />PLANT RECYCLE PUMP STATION <br />The pretreatment recycle pump was modified by <br />installing an oil system to lubricate lowerbearings. <br />RETURN ACTIVATED SLUDGE <br />PUMPS <br />Within the first year of operation, the clutches on <br />two of the return activated sludge pumps failed <br />because of an inadequate anti-reverse clutch de- <br />sign. Whenexamined, the manufacturerfound the <br />clutches needed a modification that would allow <br />properlubrication.Maintenance staffdisassembled <br />the pumps, shipped them to the manufacturer, <br />then reinstalled the modified parts; the manufac- <br />turerpaid all modification expenses. <br />Near the end of the first year of operation, mainte- <br />nance staff found defective anti-reverse couplings <br />Page 49 <br />in the return sludge pumps. They were replaced <br />with the help of the manufacturer. <br />During the first year of operation, a pump shaft on <br />a return activated sludge pump broke from the <br />excessive torque resulting when the pumps started <br />at full speed. Instrument technicians redesigned <br />the lead/lag controls for the pumps, and a ramp star <br />was installed to allow the pumps to reach full speed <br />more gradually. <br />DISSOLVED AIR FLOTATION (DAF) <br />THICKENER <br />During the process of thickening waste activated <br />sludge, the drive chain for the flotation thickener <br />broke down several times. Each breakdown took <br />approximately nine hours to repair. The break- <br />downs occurred after a new timed on/off control <br />had been installed in the flights. Once staff mem- <br />bers discontinued use of the timer control, they <br />experienced no further problems. The collector <br />flights now run continuously under variable speed <br />control. <br />DISINFECTION~DECHLORINATION <br />EQUIPMENT <br />During maintenance of the chlorinators, <br />sulfonators, and evaporators at final treatment <br />over the last five years, staff has replaced all regu- <br />lators, gauges, diaphragms, and pressure vessels. <br />TURBIDITY METER <br />Staff installed a meter that continuously monitors <br />final treatment turbidity. <br />WZ SYSTEM <br />In the second year of operation, several major <br />failures of W2 pumps occurred. The lowerbearings <br />of the magnetic clutch failed, creating enough heat <br />to melt the slip-ring assembly. The problem oc- <br />curred because the manufacturer's lubricant was <br />unable to withstand the heat of the magnetic <br />clutch. Staff switched to ahigh-temperature lubri- <br />cant, but the clutch coil failed in one pump, and <br />the electronic drive bearingfailed in anotherpump <br />only one month after service. Less than a year later, <br />the same pump bearing failed again. The plant <br />purchased a new, larger end bell with two new <br />
The URL can be used to link to this page
Your browser does not support the video tag.