Page 38 Section E: RESIDUALS MANAGBMENT FACIIdTIBS OPERATIONS <br />• Well Water Irrigation <br />The first year fescue grass seedlings were too small <br />and delicate to tolerate the low pH cannery efflu- <br />ent. Toensure the sensitive plants survived, irriga- <br />tion water was drawn from a well and pumped to <br />the aeration basin, where it was withdrawn by the <br />irrigation pumps. This was the first use of the <br />center pivot irrigation equipment. <br />• Programmable Controller <br />The design of the irrigation system included pro- <br />grammable logic controllers to operate the four <br />center pivot irrigation units. During start-up, a <br />problem with the original programming was dis- <br />covered.The four center pivots would only operate <br />sequentially. A pivot would make one pass across <br />the field then have to shut down before another <br />pivot could start up. This resulted in excessive <br />startingandstoppingof thepivots, irrigationpumps, <br />and other related equipment. The crops needed to <br />be irrigated with larger quantities of water over <br />longer periods of time to allow the water to perme- <br />ate through the soil to the roots. The controller <br />was reprogrammed to reduce the cycling of equip- <br />ment. <br />• Chlorination <br />The facility was equipped with chlorination equip- <br />ment that used one-ton tanks of chlorine to con- <br />trol the odors from waste flow irrigation. The <br />operations staff tested the system during the start- <br />up season and concluded it could not be used <br />continuously. They found that applying chlorine <br />did not produce a noticeable reduction of odors <br />during irrigation, even when higher rates were <br />applied. Also, using large amounts of chlorine was <br />likely to produce organic halogen compounds, <br />formed by the chemical reactions of chlorine and <br />organic compounds. (Organic halogens are unde- <br />sirable because some, such as trihalomerhane, are <br />carcinogens.) Staff found that well-planned waste <br />handling and irrigation practices were more effi- <br />cient and reliable than chemicals in controlling <br />odors. <br />• Pump Station Instrumentation <br />Other problems with the new equipment were not <br />so easily identified and required persistence and <br />methodical problem solving to resolve. For ex- <br />ample, one incident involved an alarm at the <br />Agripac pump station. Operators would receive <br />frequent alarms that a wet well was ovelflowing, <br />but when checked, the well would be operating at <br />a normal level. Staff finally found the problem was <br />in the sonic level sensing device. The waste enter- <br />ing the tank would produce a surface foam that <br />absorbed the sonic waves instead of reflecting <br />them to the water level sensing device. The water <br />would rise until the tank overflowed, carrying off <br />enough foam for the sensing device to receive the <br />signal to start the pumps. Everything would be <br />back to normal by the time an operator arrived. <br />The sonic level detector was eventually replaced <br />with a combination of bubble tube and float-ball <br />level detectors. <br />MAJOR PROJECTS, EVENTS, AND <br />INCIDENTS <br />OnJuly3,1984, thefirstcannerywastewaspumped <br />into the storage lagoon. The following month, the <br />irrigation system was operational and the CWMF <br />began irrigating well water onto grass seedlings. <br />Cannery effluent was irrigated for the first time in <br />September 1984. Some of the problems and im- <br />provements made since that time are as follows: <br />• Center Pivot Field Ruts <br />The center pivot wheels of the irrigation system <br />caused a problem when they cut deep ruts into the <br />fields where they tracked. In some locations, the <br />ruts were nearly two feet deep. At about two feet, <br />the centerpivot would bottom out and fail. Before <br />beginning the second year of operation, the ruts <br />were filled with hog fuel or straw. Staff found that, <br />although straw was less expensive, it could not <br />support the pivots and did not work in wet field <br />conditions. Hog fuel has continued to be used as a <br />filler when ruts develop. Now that a firm soil base <br />hasbeenestablished,the amountof hogfuelneeded <br />is less each season. <br />• Preventive Maintenance Program <br />In November 1985, staff implemented a preven- <br />tive maintenance program for the CWMF. Equip- <br />ment that needed preventive maintenance .was <br />identified and labeled. Preventive maintenance <br />tasks were documented by description and fre- <br />quencyandimplementedinto theregionalfacility's <br />preventive maintenance program. <br />• Storage Lagoon Leak Tests <br />The storage lagoon has successfully passed each of <br />the annual leak tests required by the permit. With <br />over six years of operation without a leak, we <br />expect the renewed discharge permit to reduce the <br />