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Eugene/Springfield Water Pollution Control Facility 1984-1991
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Eugene/Springfield Water Pollution Control Facility 1984-1991
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6/5/2009 11:34:05 AM
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PW_Exec
PW_Division_Exec
Administration
PWA_Project_Area
Miscellaneous
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Water Pollution Control Facility
Document_Date
7/31/1993
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Page 16 <br />Section D: PLANT OPBRATIONs <br />ata time. The solutionwas the creation of aprocess <br />control committee comprised of the two supervi- <br />sors and representatives from each of the four <br />crews. This change made it possible for ideas and <br />recommendations to be more easily communi- <br />catedand acted on, and the entire staff was willing <br />to "buy in" to control strategies and guidelines. <br />^ WASTE DISCHARGE PERMIT <br />The Operations work group has operated the 49- <br />MGD activated sludge plant under two different <br />discharge permits since plant start up in April <br />1984. <br />For the first six months of operation, the plant was <br />allowed to function under the same permit that <br />regulated waste from the old Ciry of Eugene trick- <br />ling filter plant. That permit limited average <br />monthly effluent to 30 milligrams per liter (mg/L) <br />biological oxygen demand (BOD) and 30 mg/L <br />total suspended solids (TSS), except during peri- <br />ods when the Agripac Cannery waste flow ex- <br />ceeded 10 percent of total plant flow, when efflu- <br />entlevels could go up to 40 mg/L BOD and 55 mg/ <br />L TSS. <br />In October 1984, a new, more restrictive discharge <br />permit went into effect. The new permit limited <br />average monthly effluent to'10 mg/L BOD and 10 <br />mg/L TSS with no detectable chlorine residual <br />May through October and 30 mg/L BOD and 30 <br />mg/L TSS with dechlorination not requiredfor all <br />other months. <br />That permit was to have expired in July 1988 but <br />was extended by the DEQ to allow negotiations <br />between the DEQ and the MWMC on proposed <br />changes to limits and other permit language. <br />The activated sludge plant has consistently oper- <br />atedwithin its BOD and TSS permit limits. Sum- <br />mereffluent has averaged 7 mg/L BOD and 4.5 mg/ <br />L TSS. Wintereffluenthas averaged 10 mg/L BOD <br />and 8 mg/L TSS. <br />^ PLANT START-UP ACTIVITIES <br />Operations played a major role in the preparation <br />and start-up of the new facility, performing a full <br />schedule of work activities a year before the plant <br />went online. Operators had to take considerable <br />time from their work to attend training on the <br />equipment and processes of the new plant. Mean- <br />while, they had to continue operating the old <br />Springfieldplantuntflthe new plantwent on-line. <br />They also had to operate the old Eugene plant after <br />start-up of the new plant until the new processes <br />were stabilized. Only then was the entire flow from <br />the regional area introduced to the new facility. <br />TRAINING <br />Operations personnel required extensive training <br />in the new equipment and processes to be used in <br />the regional plant. The training plan took advan- <br />tage of every possible resource, including outside <br />instructors, equipment suppliers, and in-house <br />expertise. (See Training chapter.) <br />DRY READINESS CHECK <br />Much of the preparation for start-up was per- <br />formed by operators and included dry readiness <br />checks on equipment, gates, and valves. Many <br />valves had to be located because they had been <br />buried by construction activities. In addition, op- <br />erators had to tag equipment and valves for iden- <br />tification and record-keeping purposes. When all <br />discrepancies were corrected, the plant was ready <br />for clean-water testing. <br />CLEAN-WATER TESTING <br />Clean-water plant testing occurred in two phases. <br />The first phase involved afull-scale, simulated <br />operation of treatment process using river water. <br />The second phase included more detailed testing, <br />using the river water that remained in unit pro- <br />cesses. <br />The first phase began in December 1983, then <br />river water was pumped through the plant at a rate <br />of 21 MGD. Several problems were identified. <br />Operators learned that the plant influent screw lift <br />pumps could not perform at the required levels <br />without an oil cooling sys tem. They also found that <br />the pumps needed a redesign of the bearing lubri- <br />cation system, and one of the 200-HP motors <br />needed rebuilding. In addition, they discovered <br />
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